*AMERICAN AIRLINES has announced that it will cease service between Chicago OHare and Lehigh Valley, Pennsylvania and Charlotte, West Virgina. The change is effective August 23. With this change, AA will no longer serve Lehigh Valley, however it still will offer service to Charlotte, WV, from New York La Guardia.
*Mexico's VOLARIS has filed an application with the US DOT to begin passenger flights between Morelia, Mexico, and Chicago Midway. No start-up date or frequency was noted in the application.
*Airbus is cancelling its A320 freighter conversion program, and said it has started to dissolve its partnership with Russian aerospace firms United Aircraft and Irkut. The airframer cites "more demand" for passenger twinjets in the sector and not enough for the cargo version.
*AIR INDIA Pilots have sent a letter to India's DGCA saying that they should not be held responsible for accidents caused by stress in the cockpit. The letter was sent after the Pilots were denied performance-related incentives, which account for 90% of their salaries. The Pilots were paid only 10% of their salaries for March and April, and their entire pay for the month of May is still pending. The letter requests that the DGCA intervene in the matter.
*Airservices Australia has announced that effective immediately, passenger aircraft flying into Hobart and Launceston Airports in Tasmania, will be supervised by air traffic controllers 24 hours a day, 365 days a year. Officials said that after about 10:00pm, when the day's final services are scheduled to land, all local air traffic would then be monitored from radar screens in Melbourne, until the next morning. Previously, after 10:00pm, Pilots were forced to radio their positions to each other to maintain separation.An April 2008 incident, in which a VIRGIN BLUE and JETSTAR aircraft got too close for comfort on a foggy night over Launceston, triggered investigations, which ultimately led to this change.
*TURKMENISTAN AIRLINES Flight 732, a Boeing 737, rejected takeoff from Saint Petersburg, Russia, yesterday, June 3, when the left hand engine did not perform as expected during engine acceleration. The crew was able to slow the aircraft on the runway and taxi to the apron. According to media reports, the 737 most likely ingested a bird or another type of foreign object into the engine. The aircraft was removed from service for inspection and a replacement aircraft was dispatched for the flight to Ashgabat, Turkmenistan.
*GO AIR Flight 341, an A320, was ordered to go-around, just prior to landing in Patna, India, yesterday, June 3. According to media reports, the flight crew on the Airbus, inbound from Delhi, India, aborted the landing and went full throttle to ascend from a height of 500ft following an emergency command from the air traffic control. Airport sources told local media that the aircraft was positioned on a flawed approach path and it would have overshot the runway and crashed had it landed. The aircraft landed without incident on its 2nd approach. India's DGCA is investigating
*QANTAS Flight 52, a Boeing 747, had to make an emergency return to Singapore, yesterday, June 3, after the crew could not fully retract the landing gear. The 747, bound for Brisbane, Australia, landed safely back in Singapore, about 50 minutes after its initial departure. The aircraft was repaired and departed for Brisbane, early this morning, about 14 hours behind schedule. The carrier is investigating as the incident aircraft, registration VH-OJI, had just returned to service after spending 4 weeks in Hong Kong for required major maintenance.
*SOUTHWEST AIRLINES Flight 2353, a Boeing 737, had to make an emergency return to Nashville, Tennessee, on Thursday, June 2, due to a bird strike. While climbing out of Nashville, the crew reported that a large bird had struck the aircraft just above the cockpit windshield, as they climbed thru 1600 feet. The crew leveled off at 7000 feet, before landing safely back in Nashville, about 20 minutes after their initial depature. The aircraft suffered minor damage in the incident, however it was cleared to resume service, thus it departed once again for Cleveland, Ohio, after about 90 minutes on the ground.
*MORNINGSTAR Flight 7050, a Boeing 757 on Cargo Service from Toronto, ON, to Winnipeg, MB, Canada, had to make an emergency return to Toronto, on Wednesday, June 1, when the aircraft suffered a hydraulics leak while enroute. The 757 landed safely back in Toronto and was inspected. The flexible hydraulic lines to the center reservoir were found chafed and failed. The lines were replaced and the aircraft was returned to service. According to the Canadian TSB, the carrier inspected all of the flexible hydraulic lines in its Boeing 757 airliners.
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